%0 Journal Article %T Increasing drying efficiency by modifying the design of feed chute of the Gol-e-Gohar pelletizing plant ball mill %J Journal of Mining and Environment %I Shahrood University of Technology %Z 2251-8592 %A Ghasemi, A.R. %A Hasankhoei, A.R. %A Razi, E. %A Parsapour, Gh.A. %A Banisi, S. %D 2019 %\ 01/01/2019 %V 10 %N 1 %P 213-221 %! Increasing drying efficiency by modifying the design of feed chute of the Gol-e-Gohar pelletizing plant ball mill %K Pelletizing Plant %K Dryer %K Feed Chute %K Falling Location %K KMPCDEM© %R 10.22044/jme.2018.7447.1599 %X Pelletizing plant of the Gol-E-Gohar mining and industrial company consists of a burner, a dry ball mill (6.2 m × 13 m), and an air separator. The ball mill consists of a 2 m-long drying and an 11 m-long grinding chambers. The iron ore concentrate is fed to the drying chamber by a feed chute. It was found that when the feed moisture content increased from 1.3% to 3.5%, the throughput decreased by 12% (35 t/h) indicating a low performance of the dryer. Monitoring the wear rate of flights for a period of 12 months showed that the first 0.8 m (59%) length of the dryer length did not experience any wear. To overcome this problem, various feed chute designs with different geometries were simulated by the KMPCDEM© software. With the aim of arriving at a proper material trajectory, where the total length of the dryer is used, a new feed chute was selected. The simulation results indicated that if the height of the feed chute is increased from 1.60 to 2.26 m and the slope is increased from 45 to 48 degrees the material arrives at the first 0.48 m of the drying chamber. In this manner, the unused part of the drying chamber decreases from 59% to 36% of the length. After installation of the new feed chute during a period of three months, the throughput increased by 36 t/h. %U https://jme.shahroodut.ac.ir/article_1322_c32d7e94c557213d6d053917ba0231a2.pdf